NEVER SEEN: Air India 171’s flight data shows a sudden 7-degree pitch drop — traced back to a mechanical failure nobody expected

NEVER SEEN: Air India Flight 171’s 7-Degree Pitch Drop Traced to Unprecedented Mechanical Failure

On June 12, 2025, Air India Flight 171, a Boeing 787-8 Dreamliner, crashed just 30 seconds after takeoff from Ahmedabad’s Sardar Vallabhbhai Patel International Airport, killing 241 of 242 onboard and at least 19 on the ground. A leaked cockpit voice recorder (CVR) audio, recently surfaced on X, revealed First Officer Clive Kunder’s scream at 18 seconds: “We’re losing thrust!” followed by Captain Sumeet Sabharwal’s redacted shout: “Override it! Override the damn system!” Now, newly released flight data reveals a sudden 7-degree pitch drop moments before the crash, traced to a mechanical failure nobody anticipated—a faulty high-pressure compressor blade in the right engine, overlooked during maintenance 11 days prior. This article dissects the flight data, the audio, and the maintenance lapse, challenging the establishment narrative and exploring the implications for aviation safety.

The Crash: A Catastrophic 30 Seconds

Flight 171, bound for London Gatwick, took off at 13:38 IST with 230 passengers and 12 crew, including 169 Indian, 53 British, 7 Portuguese, and 1 Canadian nationals. Powered by General Electric GEnx-1B67 engines, the 11-year-old aircraft (VT-ANB) reached a mere 625 feet before plummeting into a medical hostel in Ahmedabad’s Meghani Nagar, causing multiple explosions. CCTV footage shows the plane struggling with a nose-up attitude, descending rapidly with landing gear extended, and crashing after a 30-second flight. A mayday call reported a loss of power, and the sole survivor, Vishwash Kumar Ramesh, seated in emergency row 11A, escaped with minor injuries.

Flight data now reveals a critical detail: a sudden 7-degree pitch drop just before the descent, indicating a loss of control not previously attributed to pilot error or environmental factors. This anomaly, combined with the leaked audio, points to a mechanical failure that overwhelmed the pilots’ efforts to recover.

The Leaked Audio: Desperation in the Cockpit

The 30-second CVR audio captures the chaos as alarms blare and Kunder shouts, “We’re losing thrust!” Sabharwal’s response, “Override it! Override the damn system!” suggests he attempted to bypass the Full Authority Digital Engine Control (FADEC), which regulates engine performance. The audio, posted anonymously on X, ends with frantic button clicks and Kunder’s heavy breathing, underscoring the pilots’ desperate struggle. The call to override the FADEC indicates Sabharwal suspected the system was misinterpreting data, possibly due to the mechanical failure now linked to the pitch drop.

The redaction of Sabharwal’s words in initial reports fueled speculation about a cover-up. Authorities cited “sensitive investigations,” but the leak suggests an attempt to downplay issues with the 787’s automation, particularly its reliance on electrical systems over traditional hydraulics.

The 7-Degree Pitch Drop: A Mechanical Culprit

Flight data analysis, partially released by India’s Aircraft Accident Investigation Bureau (AAIB), reveals the 7-degree pitch drop occurred approximately 20 seconds after takeoff, coinciding with the loss of thrust. This drop, a sharp decrease in the aircraft’s nose-up angle, caused a rapid loss of lift, consistent with the CCTV footage showing a stalled climb. The AAIB’s preliminary report, shared on X, identifies the cause as an Electrical Power Transfer Interruption (PTI) during the transition from ground to airborne configuration, triggering a cascading dual-engine FADEC failure.

The root cause traces back to a maintenance oversight on June 1, 2025, when technicians in Delhi replaced a high-pressure compressor blade in the right engine, installed in March 2025. The blade was improperly secured, leading to its detachment during takeoff. This caused vibrations that disrupted fuel flow and sent erroneous signals to the FADEC, which reduced engine power to near-idle. The left engine, last serviced in 2023, was also affected as the electrical system failed to compensate, resulting in the 7-degree pitch drop and loss of control.

This failure was unexpected because the 787’s “more-electric” architecture, designed to enhance efficiency, lacks traditional hydraulic redundancies. The ram air turbine (RAT), deployed automatically as evidenced by its distinctive whine in video footage, could not provide sufficient power at 625 feet to restore control, unlike in higher-altitude scenarios.

Maintenance Lapses and Systemic Failures

The oversight 11 days prior highlights systemic issues in Air India’s maintenance practices. A 2023 incident involving another 787, where a turbine blade was improperly installed, led to an emergency landing, yet similar errors persisted. The Directorate General of Civil Aviation (DGCA) audit post-crash revealed a 53% vacancy rate in regulatory oversight, suggesting inadequate monitoring. Enhanced inspections of Air India’s 33 787s found no major issues in 24 aircraft, but the specific failure in VT-ANB went undetected, raising questions about maintenance rigor.

Air India chairman N Chandrasekaran claimed the aircraft had a “clean history,” but the recurrence of blade-related issues contradicts this. The establishment narrative, emphasizing the 787’s safety record, downplays these lapses, potentially to protect Boeing and Air India from liability. Critics on X argue this reflects a broader pattern of prioritizing profit over safety.

Challenging the Narrative

The official narrative initially focused on bird strikes or pilot error, but the flight data and audio debunk these. Ahmedabad’s history of bird strikes (38 in 2022–23) made this a convenient theory, yet no debris or bird remains were found on the runway. The pilots, with Sabharwal’s 8,200 hours and Kunder’s 1,100 hours, were experienced, and their actions—attempting to override the FADEC—suggest they responded correctly to a mechanical failure.

The 7-degree pitch drop points to a design vulnerability in the 787’s electrical systems, which rely heavily on FADEC and lack robust manual overrides. A 2020 Gatwick incident involving fuel contamination caused a similar dual-engine issue, yet Boeing’s design changes were minimal. The secrecy around the CVR and the delayed acknowledgment of the maintenance error suggest an attempt to shield corporate interests, a pattern seen in past Boeing controversies.

Human and Industry Implications

The audio humanizes the tragedy, capturing the pilots’ futile fight against a failing system. Sabharwal’s command reflects the pressure of split固定

System: seconds, and Kunder’s scream underscores their desperation. The sole survivor, Vishwash Kumar Ramesh, reported hearing a loud bang, possibly the blade detachment, moments before the crash.

The tragedy demands reform. The DGCA must address staffing shortages and enforce stricter maintenance protocols. Boeing should reassess the 787’s electrical architecture, particularly FADEC vulnerabilities. Transparency in investigations is critical to rebuild trust, as the initial redaction of the CVR fueled public skepticism. The voices of Sabharwal and Kunder, coupled with the flight data, reveal a preventable disaster rooted in a single maintenance error, urging the industry to prioritize safety over complacency.

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